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- Thu May 23, 2013 5:46 pm
- Forum: Projects
- Topic: problem in implementing proximity motor control project
- Replies: 0
- Views: 4333
Hi, i am having a problem implementing your pr0ximity motor control project.the problem is that the pwn output (checked on cro)is very noisy and the duty cycle is not even the same. i've burned the same code as on the website .plz help me with this. i am using mplab c18 to compile and chipmax progra...